[version en cours de rédaction] | [version en cours de rédaction] |
Ligne 21 : | Ligne 21 : | ||
Disabled alarm for Ipull out - this was a misleading error when it is loading to gripper | Disabled alarm for Ipull out - this was a misleading error when it is loading to gripper | ||
− | = Tuning X axis drive = | + | =Tuning X axis drive= |
Following error on X axis stopped the axis on loading | Following error on X axis stopped the axis on loading | ||
Ligne 44 : | Ligne 44 : | ||
Set at 100%. Seems to easy | Set at 100%. Seems to easy | ||
+ | |||
+ | = Spindles = | ||
+ | invert300Hz=1 | ||
+ | |||
+ | InverterOkHigh=1 | ||
+ | |||
+ | Input In_InvOk mapped to 90 and configured in alarms | ||
+ | |||
+ | ringType=Mk3with DP | ||
+ | |||
<br /></translate> | <br /></translate> | ||
{{PageLang | {{PageLang |
Notes on issues encountered with Microline transfer to TwinCAT3 setup
Auteur Gareth Green | Dernière modification 21/09/2022 par Gareth Green en cours de rédaction ⧼frevu-button-review-label⧽
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Notes on issues encountered with Microline transfer to TwinCAT3 setup
The infeed 2007 does not have a LOADD sensor.
Confusion over how the code can handle this. It must have worked ok on other infeeds like this (eg Z046).
When investigating in the code, errors found on function blocks fbMotorConvey on inputs to
iArrayError
bNoSensorsCovered
iMeasureErrorMsg
These normally connect to fbArrayMeasure function block, but this does not exist in MHInfeed_2007
Disabled alarm for Ipull out - this was a misleading error when it is loading to gripper
Following error on X axis stopped the axis on loading
When tuning took place, the bar was not clamped
Tried a reversing move with clamps on.
At Speed 10, following error was 0.2
At speed 50, following error was 1
At speed 100, the following error was 2mm
This shows a proportional increse in following error as spee increases
Tried changing drive P-Gain, no effect
Changed 3.02 Kff Gain (feed forward. Was on zero
Following error dropped proportionally to ff gain 0-100%
Set at 100%. Seems to easy
invert300Hz=1
InverterOkHigh=1
Input In_InvOk mapped to 90 and configured in alarms
ringType=Mk3with DP
en
none
0
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